<_x0034_00993129>
400993129 05A 100264 XTO ENERGY INC
382 CR 3100
AZTEC NM 87410 Dee Johnson 505 333-3164 Dolena Johnson Sr. Regulatory Analyst 2016-02-19T14:14:03.157-07:00 DRAFT johnsond 2016-02-19T14:14:03.157-07:00 johnsond dee_johnson@xtoenergy.com 0.00000 dee_johnson@xtoenergy.com johnsond johnsond 2016-03-10T07:39:29.187-07:00 400993129 05 067 05224 00 LA PLATA UTE 1 NESW 36 33N 7W N IGNACIO BLANCO 38300 400993129 This is a Record Cleanup being done on historical work from 2006. I have not broken out the frac data since the work was done prior to the 2012 rule change. 400993129 400993129 FORM 5A SUBMITTED 400993129.pdf 400993129 401001748 OPERATIONS SUMMARY Ute 01 - Summary Rpt 2006 DK P&A - MV RC.pdf 34448 400993129 401001749 WELLBORE DIAGRAM Ute 1 Updated Wellbore Diagram.pdf 140528 400993129 CLFH 4997 5004 4 0.34 2006-04-13T00:00:00-06:00 CM 400993129 DKTA N 7425 7610 Y Fish in hole. Please see attached wellbore diagram showing the details. 2006-03-31T00:00:00-07:00 N 7140 2 AB 400993129 LWIS Y 4669 4895 9 0.34 N Acidized w/609 gals 15% NEFE ac w/25 Green Bio-Balls. 5 gals 15% HCl. Flshd w/53 bbls 2% KCl. Frac was cancelled. 2006-04-15T00:00:00-06:00 24 0 320 0 FLOWING 495 357 1 988 SOLD 8 0 64 320 0 2 5247 3 8 DRY 2006-04-11T00:00:00-06:00 2006-04-13T00:00:00-06:00 2006-04-13T00:00:00-06:00 PR 2006-04-11T00:00:00-06:00 FRACTURE STIMULATION 400993129 ME-PL Y 4997 5301 56 0.34 N Acidized w/2053 gals 15% NEFE ac w/150 Green Bio-Balls and 5 gals 28% HCl ac. Frac'd w/140,798 gals 65% gual 12# Delta Foam 140 frac fld carrying 123,303# 20/40 Brady sand. Flushed w/3748 glas 12# linear gel. 2006-04-15T00:00:00-06:00 24 0 320 0 FLOWING 495 357 1 988 SOLD 8 0 64 320 0 2 5247 3 8 DRY 2006-04-04T00:00:00-06:00 2006-04-13T00:00:00-06:00 2006-04-13T00:00:00-06:00 PR 2006-04-06T00:00:00-06:00 FRACTURE STIMULATION 400993129 MENF 5032 5155 14 0.34 2006-04-13T00:00:00-06:00 CM 400993129 PNLK 5189 5301 38 0.34 1962-06-01T00:00:00-06:00 CM Thread was being aborted.