<_x0034_00407595>
400407595 05 100322 NOBLE ENERGY INC
1625 BROADWAY STE 2200
DENVER CO 80202 Julie Webb 720 587-2316 Julie Webb Regulatory Analyst 2013-04-22T14:27:58.907-06:00 DRAFT webbj 2013-04-22T14:27:58.907-06:00 webbj juliewebb@nobleenergyinc.com 0.00000 juliewebb@nobleenergyinc.com webbj webbj 2013-04-22T14:38:58.777-06:00 400407595 05 123 12859 00 WELD STATE-FARM 36-6 SENE 36 5N 65W 6 1980 FNL WATTENBERG 660 90750 FEL 68091 1985-12-03T00:00:00-07:00 1985-12-12T00:00:00-07:00 1985-12-13T00:00:00-07:00 OW 7160 7122 4762 4773 Gamma Ray CCL/CBL true Final Completion 400407595 Gamma Ray CCL/CBL hard copy mailed. 400407595 400407595 FORM 5 SUBMITTED 400407595.pdf 400407595 400407608 CEMENT JOB SUMMARY State Farm 36-06 Cement Summary.pdf 234067 400407595 1ST 7 7 8 4 1 2 15.1 7155 150 7160 6400 0 CBL ACTUAL 400407595 SURF 12 1 4 8 5 8 24 306 210 306 0 0 CALC ACTUAL 400407595 19057 S.C. 1.1 191 0 508 400407595 cement work 2013-02-04T00:00:00-07:00 400407595 cement work Control well w/ 20 bbls kill fluid. RIH w/ blade bit, and scraper, 227jts. Tagged fill at 7096’ KB. TIH w/ RBP, retrieved head, 211 jts 2 3/8” tubing. Set RBP @ 6571’ KB w/ 211 jts. Toll hole clean. Pressure test to 1000#. Spot 2sks sand on plug. Unland casing. Pick Up mule shoe and TIH w/17 jts of 1 ¼“to 539’. Pump 191 sks of “G” neat 15.8 ppg cement from 508’ to surface. Reland casing. Bond log from 750’ to surface. RIH w/ retrieving head and establish circulation and latch onto RBP. Roll hole clean and release RBP. Land 2 3/8” 4.7 # J-55 tubing to 7009.12’ KB. Rig down and move off. Thread was being aborted.