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400383904 05 100322 NOBLE ENERGY INC
1625 BROADWAY STE 2200
DENVER CO 80202 Julie Webb 720 587-2316 Julie Webb Regulatory Analyst 2013-02-21T14:17:03.833-07:00 DRAFT webbj 2013-02-21T14:17:03.833-07:00 webbj juliewebb@nobleenergyinc.com 0.00000 juliewebb@nobleenergyinc.com webbj webbj 2013-02-25T08:30:50.12-07:00 400383904 05 123 10500 00 WELD LUNDVALL 1 NESW 18 5N 66W 6 1920 FSL WATTENBERG 1920 90750 FWL 64025 1981-12-19T00:00:00-07:00 1982-01-12T00:00:00-07:00 1982-01-14T00:00:00-07:00 OW 7986 7710 4920 4925 Gamma Ray CCL/CBL true Final Completion 400383904 Gamma Ray CCL/CBL hard copy mailed 400383904 400383904 FORM 5 SUBMITTED 400383904.pdf 400383904 400383985 CEMENT JOB SUMMARY Remedial Cement Job Summary.pdf 722715 400383904 1ST 7 7 8 5 1 2 14/15.5 7985 500 7986 6330 0 CBL ACTUAL 400383904 SURF 12 1 4 8 5 8 24 218 125 218 0 0 CALC ACTUAL 400383904 17342 S.C. 1.1 PERF & PUMP 551 300 5 591 400383904 cement work 2012-10-02T00:00:00-06:00 400383904 cement work Control well w/ 30 bbls kill fluid. RIH w/ 2 3/8” bit and scraper 234 jts. Tag fill at 7397’. Roll hole clean . POOH with tubing PU 5 ½" WLTC RBP set @ 7279’ KB w/ 230 jts. PSI test csg to 1000#, no loss. Bond log from 6330 to surface. TOC is at 6130’. RIH w/ sqz guns to 551 and shot 2 holes. Test iron to 3000 psi. Pump 3.5 bbls spacer ahead. Pump 300 sks of “G” neat 15.8 ppg cement from 591’ to surface. PU 4 ¾” cone bit and 3 ¾” dill collats and TIH tag cement at 420’. Drill out to 510’. Roll hole clean. Test hole to 500 psi, good test. Run Bond log form 750’ to surface. Annular cement bottom is at 586’ with excellent bond to surface. RIH w/ retrieving head and establish circulation and latch onto RBP. Roll hole clean and release RBP. Land 2 3/8” J-55 tubing to 7398’. Rig down and move off. Thread was being aborted.