COGIS - Spill Reports

Form 19/19A                                                                     Doc
Date Rec'd: 6/7/2010 Report taken by:   Robert Chesson
DocNum: 2607162 API number:   05-013-06423 Facility ID:

 206928

Operator Information

Operator: NOBLE ENERGY PRODUCTION INC Oper. No. 10120
Address: 1625 BROADWAY STE 2200 ATTN: TED BROWN  DENVER , CO 80202
Phone: (303 )389-3600 Fax: (303 )595-7403
Operator Contact: MARTY  FARAGUNA

Description of Spill:

Date of Incident: 6/4/2010
Type of Facility: WELL
Well Name/No. ANDERSON  MB 33-1 Fac. Name/No.  
County Name: BOULDER
qtrqtr: NENE section: 33 township: 2N range: 69W meridian: 6
Volumes spilled and recovered (bbls)
Oil spilled:    Recvrd:    
Water spilled:    Recvrd:    
Other spilled:    Recved:    
GW Impact? Y Surface water impact? N Contained within berm? N
Area and vertical extent of spill:  - X   -
Current land use:  CROP
Weather conditions:  CLEAR, DRY
Soil/Geology description  COLBY SILTY CLAY LOAM
Distance in feet to nearest surface water:  170
Depth to shallowest GW:  
Wetlands:   Buildings:  1000
Livestock:   Water Wells:  600
Cause of spill:
EQUIPMENT FAILURE

Immediate Response:

PRODUCTION SHUT IN.

Emergency Pits:

ESTABLISHED A CONE OF DEPRESSION TO PULL OIL AND WATER AND TRANSFER TO DISPOSAL.
How extent determined:
EXTENT OF CONTAMINATION WILL BE DETERMINED VISUALLY AND BY PHOTO-IONIZATION DETECTOR READINGS DURING EXCAVATION OPERATIONS.
Further Remediation
REMEDIATION ACTIVITIES WILL INCORPORATE EXCAVATION OF SOILS AND TREATMENT OF GROUNDWATER.

Prevent Problem:

BATTERY WILL BE RECONSTRUCTED WITH NEW LINES.

Detailed Description:

OIL DUMP LINE CORRODED AND LEAKING.

Field Visit/Follow Up

Name

Phone

Date

No Field Visit data found.


Final Resolution
Date Case Closed? Letter Sent? COGCC person
6/7/2010 Y Robert Chesson

5/22/2013 Y N

SEE REMEDIATION #5135, FORM 27 #2607988


Thursday, August 22, 2019